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(Research Notes: This “History of flight” official
record is part of the releasable portion of the TB-25N Aircraft Mishap Report, 31 January 1956 received regarding
a Freedom of Information Act (FOIA) request of 18 March 1994. When this document is compared side-by-side with another copy
received by another individual during a separate FOIA request, different sections have been “blacked out” or censored.
Areas highlighted in yellow were blacked out in one copy only. Information
designated by “XXXXXX” has been blacked out in both versions of the same document. Every effort
has been made to faithfully reproduce this text, including poor punctuation, capitalization, and misspellings.)
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53. History of flight: B-25N, No.44-29125, departed Nellis
Air Force Base Nevada on 30 January 1956. The purpose of the flight was aircraft
parts pick-up at Olmsted Air Force Base Pennsylvania, and delivery of two passengers to Andrews Air Force Base Maryland. The crew consisted of Major William L. Dotson, pilot, Captain John F. Jamieson, pilot,
Captain Steve W. Tabak, pilot, Staff Sergeant Walter E. Soocey, Crew Chief, and Airman Second Class Charles L. Smith, Crew
Chief; Captain J.P. Ingrahm and Master Sergeant Alfred J. Alleman were listed as passengers.
The aircraft departed Nellis Air Force Base at approximately 1815E and arrived at Tinker Air Force Base Oklahoma at
2221E. The crew decided to RON at Tinker Air Force Base in view of ice and snow
reported on runways at Selfridge, the next point of destination, and brake trouble discovered on the aircraft. A new right brake assembly and left outboard brake assembly were installed.
The aircraft was refueled at Tinker Air Force Base with 560 gallons of 100 octane fuel for a total of 975 in the tanks. Flight was resumed on 31 January 1956, departing Tinker Air Force Base at 0853E and
arrived at Selfridge at 1313E. Major William L. Dotson was flying as co-pilot
on this leg of the flight with Captain Jamieson as pilot. During this flight 28" of manifold pressure and 1850 r.p.m. were utilized. Upon arrival at Selfridge Air Force Base, notification was received that approximately three hours would
elapse before refueling could be completed. It was decided to proceed to Olmsted
Air Force Base with the fuel estimated available i.e., 375 gallons, since this represented approximately 3 hours of fuel and
the flight to Olmsted would require but one hour and 40 minutes. The estimate
of 375 gallons remaining in the aircraft was computed by the Crew
Chief who indicated that not more than 600 gallons would refuel the aircraft.
The aircraft departed Selfridge Air Force Base at 1443E hours with Major Dotson as pilot and Captain Jamieson as co-pilot. Captain Ingraham and Sergeant Soocey were in the forward crew compartment; Airman
Smith and Sergeant Alleman were in the rear compartment. Captain Tabak remained
at Selfridge. The flight proceeded under IFR conditions at 7000 indicated, 1000
on top, via Red Airway 20, Red 85, and Green 4. Position reports were given by
Captain Jamieson at Windsor, Cleveland, Akron, Columbiana and Butler. The flight
was uneventful until in the vicinity of Butler radio Beacon, approximately 17 nautical miles northeast of Greater Pittsburgh. At Butler it was noted that
fuel gauges had moved noticeably for the first time. flight was being conducted
with power settings at 28" manifold pressure and 1800 r.p.m. with mixtures pulled back past the auto-lean position. With the exception of minor difficulty in holding synchronization on the right propeller, no indication
of any malfunctions were apparent up to this point. North of the New Alexandria
Beacon, approximately 31 nautical miles east of Greater Pittsburgh Airport, an obvious and unusual decrease in the fuel indication
on all tanks was noted. XXXXXXXXXXXXXXXXXXXXXXX Approximately 120 gallons were
indicated as in the aircraft at this point. Pittsburgh Center was contacted on
UHF Channel 5 and a change in destination to Greater Pittsburgh Airport was requested and received at approximately 1600E. The aircraft was advised that the weather at Greater Pittsburgh Airport consisted
of a 3000' broken ceiling with 10 miles visibility. River Radio Beacon, 5 nautical
miles east of Greater Pittsburgh Airport, was tuned in on Radio Compass at this time and the aircraft homed in on a heading
of approximately 285 degrees. A few minutes after leaving the New Alexandria
vicinity, at approximately 1603E, a large hole in the undercast was sighted and the IFR clearance was cancelled. at 1604E. The aircraft was descended through the hole to maintain more positive visual contact and avoid any possible IFR approach delay. At this time wing tanks were indicating empty; main tanks were indicating approximately 80 gallons of total
fuel remaining. A large deflection on the radio compass indicator was noted,
and close proximity to River Beacon was assumed and reported to Pittsburgh Center. The
aircraft was descended beneath the broken ceiling to approximately 3000' indicated.
(In this vicinity average terrain level is 1100 to 1200 feet.) Shortly
after descending to VFR conditions, the heavily populated fringes of the city of Pittsburgh were sighted and course was altered
to a generally southerly direction to avoid housing areas. At this time it became
evident that fuel was decreasing constantly at an abnormal rate and it was decided to attempt landing at Allegheny County
Airport, approximately 15 nautical miles southeast of Greater Pittsburgh Airport. Shortly
thereafter, at approximately 1609E, the Monongahela River was sighted and both engines ceased operating at approximately 3000'
indicated. Major Dotson advised the crew that the aircraft would be
ditched in the river. Captain Jamieson transmitted a "Mayday" which was
overheard at the Allegheny County Tower at 1609E on either 126.18Mc or 257.8Mc. Major
Dotson lowered wing flaps and completed a wheels-up touchdown, heading downstream in a generally south, southwest direction
at approximately 1610E to 1611E. The ditching was successful and all occupants
evacuated the aircraft with no apparent injuries. All six persons were able to
climb aboard the upper surfaces of the aircraft as it floated down the stream. The
Monongahela River at this point varies from 500 to 1000 feet in width; the river depth varies from 25 to 35 feet. The current was estimated to be approximately 8 to 10 knots; the recorded water temperature was 35 degrees
F; the recorded air temperature was 27 degrees F; the recorded wind velocity was 8 to 10 knots, from the northwest. The aircraft remained afloat for an estimated 10 to 15 minutes. XXXXXXXXXXXXXXXXXXXXXXX
that the aircraft was sinking XXXXXXXXXX the crew and passengers to remove their shoes
and swim to a log observed floating nearby. XXXXXXXXXXX all six persons could swim. Sergeant Alleman, Airman
Smith and Major Dotson reached the nearby log successfully; Major Dotson and Airman Smith remained with the log until recovered
by a commercial river boat, approximately 15 minutes later. Master Sergeant Alleman
reached the log but struck out for the left bank of the river. He was able to
swim ashore with great difficulty and was assisted from the water by civilians and local police officers. Captain Jamieson used a small wooden post and was able to remain afloat until recovered by a police launch.
XXXXXXXXXXXXXXXXXX Captain Ingrahm XXXXXXXXXXXXXXXX
disappear beneath the water. Sergeant Soocey was XXXXXXXXXXX on some unidentified debris when last seen. XXXXXXXXXXXXX
Subsequently, XXXXXXXXXXX Sergeant Soocey swimming toward the left bank and disappear beneath the water approximately 60 feet from the shore.
The aircraft drifted for an estimated 1 mile from the point of impact prior to sinking.
Major Dotson and Airman Smith, the last personnel to be recovered were recovered approximately 1 1/2 to 2 miles from
the scene of impact. At the time of this report neither the aircraft nor missing
personnel have been located. (Research Note:
This last sentence dates this report prior to April 8, 1956.)
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Suggested
reading
Goerman, Robert A., Thirty
Seconds over Pittsburgh, FATE magazine, May-June 2009 www.fatemag.com
Johns, Robert H., The Incident That Could Have Killed Pittsburgh,
Closson Press, September 2008 www.clossonpress.com
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